025-85283059
210003
江南,某污水厂主流Anammox现象产生的原因探讨 苑泉1, 贺北平2, 钱亮2, 宫徽1, 万硕2, 蔡虎林3, 周亚旭3, 王凯军1清华大学环境学院环境模拟与污染控制国家重点联合实验室;浦华环保有
时间:2024-01-08
焦点提醒: 某污水厂支流Anammox现象发生的缘由切磋 苑泉1, 贺北平2, 钱亮2, 宫徽1, 万硕2, 蔡虎林3, 周亚旭3, 王凯军1清华年夜学情况学院情况摹拟与污染节制国度重点结合尝试室;浦华环保无限公司;西安市污水处置无限义务公司
municipal wastewater;mainstream Anammox;A2/O-IFAS process;carrier;font-size: 10pt;">simultaneous nitrification and denitrification
A full-scale wastewater treatment plant (WWTP) located in central China was upgraded based on the original inverted A2/O process, and the A2/O-IFAS process was formed by introducing carriers in the anaerobic and anoxic tanks. After more than four and a half years of stable operation, the system showed excellent nitrogen removal efficiency, andthe reddish biofilm appeared on the carriers in anaerobic and anoxic tanks. The biofilm on the carriers in the anaerobic and anoxic tanks hadAnammox activity. The microbial community composition of biofilm and suspended sludge was analyzed by highthroughput sequencing method.Candidatus Kuenenia,the dominant Anammox bacteria (AMX) at the genus level,was concentrated in the biofilm in the anoxic tank, and its relative abundance was significantly higher than that in the biofilm in the anaerobic tank and suspended sludge. Local aeration under the screens in the anaerobic and anoxic tanks was used to prevent blocking of the carriers and promote fluidization, which made the anaerobic/anoxic system always in alternate change of low dissolved oxygen (DO).It also promoted the simultaneous nitrification and denitrification (SND) process, and provided substrates for AMX. Coexistence, symbiosis and natural competition of traditional nitrifying bacteria and denitrifying bacteria in the suspended sludge and AMX in the biofilm removed nitrogen synergically at low DO. The low DO formed by local aeration and addition of carriers in the anaerobic and anoxic tanks promoted the emergence of mainstream Anammox phenomenon and became one of the main reasons for stable operation of the system.
[1]孙永利,张维,郑兴灿,等.城镇居平易近人均日糊口污水污染物发生量测算之产污纪律[J].中国给水排水,2020,36(6):1.[2]范荣桂,刘娜,尹利鹏,等.污泥厌氧催化快速发酵产VFAs的实验研究[J].中国给水排水,2020,36(11):69.[3]镇祥华,余琴芳,万年红,等.污水处置厂二级出水深床滤池超深度脱氮研究[J].中国给水排水,2020,36(11):91.[4]赵美玲,朱涛,冯江,等.水力模子在合流制调蓄池进水管革新中的利用[J].中国给水排水,2020,36(07):114.[5]朱一文,王文亮.基在水文方式的暴雨调理塘范围计较[J].中国给水排水,2020,36(07):118.[6]李骏飞,李欢,杨磊三.粤港澳年夜湾区立异治水模式分享[J].中国给水排水,2020,36(08):1.[7]李激,王燕,熊红松,等.城镇污水处置厂消毒举措措施运转调研与优化策略[J].中国给水排水,2020,36(08):7.[8]赵锡锋,李兴强,李军.好氧颗粒污泥手艺中试研究和利用进展[J].中国给水排水,2020,36(08):30.[9]王建西.PTA2O工艺用在养猪废水处置和其Anammox现象阐发[J].中国给水排水,2020,36(08):56.[10]高海英,邓磊,侯晓庆,等.MBR工艺在西安经开草滩污水处置厂中的利用[J].中国给水排水,2020,36(08):63.[11]莫俊锋,王文亮,白献宇,等.基在设想暴雨法的CSO调蓄池池容计较方式切磋[J].中国给水排水,2020,36(08):77.[12]郭健.纳入年夜直径热力管的分析管廊设想研究[J].中国给水排水,2020,36(08):82.[13]蒙政成,冼萍,黄付平,等.NCMBR工艺在工业园区污水处置项目中的利用[J].中国给水排水,2020,36(08):88.
更新日期/Last Update:2020-06-01中国给水排水杂志社官方网所有材料均源在网上的同享资本和期刊同享,请特殊留意勿做其他不法用处 若有加害您的版权或其他有损您好处的行动,请联系指出,地方会当即进行更正或删除相关内容
论文颁发投稿邮箱:cnwater@vip.163.com
CopyRight (C)2016 中国给水排水杂志社官方网 版权所有津ICP备20004590号